- Joined
- Feb 26, 2018
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- 51
I was running a mission with waypoints using Litch and when I finished I realized that the gimbal no longer responded to TX commands. The gimbal performs initialization movements when the drone is turned on and responds to the commands on programmed missions, it also responds to IPED movements, but does not respond to the movements of the wheel responsible for the gimbal's pitch. I use a mini IPED 4. I've reconnected TX, calibrated gimbal, control, used DJI GO, sansumg ... all of the commands seem to be working, it seems like a communication problem between the pitch wheel and the drone. Does anyone know how to solve it?